Douglas pilots and engineers who were stationed in Istanbul to assist Turkish Airlines found that their job was nearly impossible and lamented that the airline wouldnt be ready to operate the DC-10s on its own for years. Quite simply, the extra weight of passengers caused the cabin floor to fail more completely than in the Windsor incident, when no passengers were seated in the area above the rear cargo hold. The locking system was mechanically upgraded to prevent the handle from being forced closed without the pins in place, and the vent door was altered to be operated by the pins, thereby indicating when the pins, rather than the handle, were in the locked position. Mr. David George Scott, 27, bakery worker Most damning of all: McDonnell Douglas and its contractors knew exactly how dangerous the failure of the cargo door could be, and deliberately stymied efforts to do something about it. Miss Helen Victoria Rumsey Neale, 38, research economists The sudden difference between the air pressure in the cargo area and the pressurised passenger cabin above it, which amounted to 2 pounds per square inch or 14 kilopascals, caused a section of the cabin floor above the open hatch to fail and blow out through the hatch, along with six occupied passenger seats attached to the floor section. The plane was diving ever more steeply toward the ground, spiraling downward faster and faster, hurtling toward the fields, forests, and villages below. Turkish Airlines (TK) Turkmenistan Airlines (T5) TUS Airways (U8) Tway Air (TW) Twin Jet (T7) Ulendo Airlink (NYS) Ultra Air (U0) UM Air (UF) Uni Air (B7) . Turkish Airlines still flies to London, but the route is currently non-stop, and flown with an Airbus A330-300. A large section of the floor near the last few rows of seats consequently failed, collapsing down into the cargo hold. After a while, the plane started giving an overspeed warning. Of the 346 passengers and crew on board, only 40 bodies were visually identifiable with rescue teams recovering some 20,000 body fragments in all. Mr. Hiroshi Tsuchiya, 23, bank management trainee Mr. Anders Sipo Qunta, 59, married, one child, doctor and his wife Margaret Mary, 60 Mr. Michael Rodney Whitehead, 32, married, two children, engineer Mr, Mohamed Saad Chaouni, 22, student, New ZEALAND The plane was a 1-year-old Mcdonnell Douglas DC-10. Instead, McDonnell Douglas issued a non-binding service bulletin reminding DC-10 operators to install the new wire and requesting that they add a placard telling ground agents not to apply more than 50 pounds of force to the locking handle. In an instant, all the air rushed out of the pressurized fuselage, blasting the cockpit door off its hinges and sucking the pilots hats back into the passenger cabin. The NTSB's investigation into Flight 96 found that the handlers had forced the locking handle closed, in spite of the fact that the latches had not engaged fully because of an electrical problem. Mr. John Frederick Slater, 33, married, steward and his wife Gloria, 31, and their daughter Nadine Nicolas, 4 The terrifying result of the mis-rigging is, however, well-established. But before the office could finish drafting even this first most insignificant directive, Jackson McGowen, president of the Douglas division of McDonnell Douglas, telephoned FAA Administrator John Shaffer in order to intervene. Strike by British European Airways Employees While the ORY-LHR leg usually did not attract many passengers, an ongoing strike by British European Airlines employees meant that the economy cabin was full, with the aircraft originally 167 passengers and 11 crew members for the first leg, 50 disembarked, and 218 more pasengers boarded. Mr. Zeki Dogan Beller, 37, married, two children, maintenance manager for THY Captain Berkz tried to pull up, but there was no response. Two months later, despite not having any concrete plans, McDonnell Douglas announced that it would build the same thing, except better, and they would get it done faster. Nine passengers were never identified. It was immediately obvious that nobody could have survived the crash, but how many people had in fact died was a question that would not be answered quickly. One of these accidents undoubtedly occurred on Turkish Airlines flight 981. On March 3, 1974, the McDonnell Douglas DC-10 operating the flight crashed into the Ermenonville forest outside Paris, killing all 346 people on board. Turkish Airlines Flight 981 was a McDonnell Douglas DC-10, registered TC-JAV and named the Ankara, that crashed in Fontaine-Chaalis, Oise, France, outside Senlis, on 3 March 1974. Mr. Motohisa Kinugasa, 22, bank management trainee Changes had also been made to the warning light switch, so that it would turn off the cockpit warning light even if the handle was not fully closed. Mr. Robert Andre Jean Lerendu, 34, married, one child, bank director and his wife Josette, 30 and their daughter Corinne Elise Simone, 5 and Mr. Lerendus brother Mr. Jacques Auguste Louis Lerendu, 38, married, two children, company secretary The young nurses and paramedics who joined the search certainly thought they were going to be treating survivors. (Unstated in either memo was the fact that Convair had little choice but to agree to Douglass design decisions.) The wreckage was so fragmented that it was difficult to tell whether any parts of the aircraft were missing. Problems with the hatches had occurred previously, most notably in an identical incident that happened on American Airlines Flight 96 in 1972. Ms. Joyce Marjorie Hope, 53, divorced, two children, film librarian and her son [2] The plane, owned by Mitsui, was originally to be purchased by All Nippon Airways, but the Japanese airline declined the aircraft in favor of the Lockheed L-1011 TriStar. [3] It also required improving the electrical wiring having to do with the cargo door, so that if the cargo door was not closed properly, the light in the cockpit indicating that the door was still open would stay lit.[3]. The aircraft is carrying 167 passengers, most of whom are Turkish. With the locking pins overlapping the flanges by only 2.5 millimeters even at full extension, and no support plate to stop the torque tube from bending, only 13 pounds (57 Newtons) of force were required to bend the torque tube and lock a door that was not fully over-center. . A member of the Star Alliance since 2008, it uses its strategic location to offer key connections to and from Europe. But the worst did not come. It was noted that the pins on the hatch that failed on Flight 981 had been filed down to make it easier to close the door, resulting in the hatch being less resistant to pressure. McDonnell Douglas thus devised a locking system which, unlike most similar systems, was not intended to keep the door shut, but simply to indicate whether it was properly closed. But, with the gift of hindsight, it is possible to say that being the first was both a blessing and a curse. And to make matters worse, the jammed rudder meant that they would have no directional control after landing. Four days after the crash of Turkish Airlines flight 981, the FAA issued a series of Airworthiness Directives mandating a redesign of the cargo door and the installation of vents in the floors of all large jets to relieve a pressure spike. of 1 As it turned out, when the hold depressurized, the passenger cabin above it did not. Mr. Mehmet Engin 1nan, 21, student and his sister Hatize Burcin, 25, student Pilots Hurt called this an interesting legal and moral problem. And in the end, he chose the legal over the moral. Nor could it have been done the stamps were dated July 18th 1972, before any instructions for the repair had even been drafted. A holding company in Japan had purchased six DC-10s with the expectation that they could up-sell them to All Nippon Airways; but due to some kind of backroom deal, that airline decided to buy the Lockheed L-1011 instead. No. Miss Danielle N Guyen Thi, 22, student, , May they rest without remorse May my deed change the way we fly Bruno Druesne. The sudden departure of the door caused all the air to rush out of the cargo compartment, taking with it a number of items, including an occupied coffin. It turned out that the sheer number of passengers probably made the difference between a repeat of the Windsor incident and the total disaster which actually occurred. Mr. Necmettin Senyurt, 24, engineer Turkish Airlines flight 981, a 4th most catastrophic aviation disaster in history, was caused by serious flaw by McDonnell Douglas, and this only disaster made a serious impact on aviation market, also the existence of the McDonnell Douglas company. An air traffic controller noted that as the flight was cleared to FL230, he had briefly seen a second echo on his radar, remaining stationary behind the aircraft, likely the remains of the rear cargo door. As Lannier rolled up beside a fire truck near the intersection of two dirt tracks deep in the forest, a firemen emerged and told him: Bodies all over the place, like. [2] An investigation after the crash found out that one of the cargo doors at the rear of the aircraft was not properly closed and secured. On March 3, 1974, a Turkish Airlines McDonnell Douglas DC-10, which operated Flight 981 between Istanbul and London, crashed in the Ermenonville forest, killing all of its 346 occupants. Miss Meral Ciril, 17, student Mr. Sydney Maurice Bressloff, 52, insurance agent Their gamble on propeller planes had failed; the DC-8 and DC-9, their belated entries into the jet market, were not selling particularly well; and escalating inefficiency on the production line had left the company struggling to fulfill orders. Mr. Keith John Madge, 25, film technician In 1967, Douglas admitted defeat. Everything that wasnt tied down rushed toward the back of the plane, where, to the immense horror of the cabin crew, a gaping hole had opened in the floor, through which clouds could be seen hurtling past at great speed. There were a total of 346 people on board, of which 335 were passengers and 11 were crew members. Mr. Carlo Alberto Fontana, 38, married, one child, engineer Miss Franoise Bernard, 2l, student Most probably someone had attempted to extend the lock tube but simply twisted it the wrong way. Mr. Nicholas Jeremy Stewart Fripp, 25, married, one child, wine merchant Although relevant sections of the Turkish Airlines board meeting minutes were redacted for national security reasons, it is thought that the Turkish Air Force wanted the DC-10s because they expected an imminent outbreak of war in Cyprus, and the DC-10 could carry 350 troops at a time into the airport in Nicosia. Turkish Airlines Flight 981 was a regular flight operated by Turkish Airlines, from Istanbul to London Heathrow, with a stopover in Paris. Mr. William Harry Deane, 59, married, one child, company director and his wife Brenda Winifred, 45 When he tried to pitch up, the elevators barely moved, and intense pressure on the control column was needed just to prevent the plane from going into a dive. The aircraft almost immediately attained a 20-degree, nose-down attitude, and started picking up speed, while Captain Berkz and First Officer Ulusman struggled to regain control. But before McDonnell Douglas could even begin drafting a proposal, rival manufacturer Lockheed announced that it would produce the L-1011 TriStar: a wide body, three-engine jet that would meet all of American Airlines specifications. Mr. Ivor John Bradley, 46, married, two children, marketing director But if it was Turkish Airlines that made the adjustments, that would not have surprised any of the Douglas employees who were charged with helping THY incorporate the DC-10 into its fleet. What happened? he shouted. The interconnecting linkage between the lock and the latch hooks had not been upgraded. We hit the ground; Ulusman said. So was it THY that mis-rigged the cargo door after the Americans went home? Miss Sukran Mihlar, 17, student Turkish Airlines Flight 981. Crew of craft TC-JAV (A detailed account here). Countless side characters stepped in and out of the picture, from the engineer who certified his own work and missed a clear design flaw, to the Turkish Air Force officials who wanted to use the DC-10 to carry troops to Cyprus, each of them unwittingly playing a small but possibly crucial role in the buildup to disaster. The majority of the passengers were British. Mrs. Georgina Evelyn Byatt, 46, married, one child, teacher Mr. Thomas Roger Marriage, 37, married, three children, farmer Mr. Loren Mell Hart, 41, married, three children, geologist and his wife Alice Jvan, 40, their son Robert Raymond, 12 and their daughters Nancy Joan, 14, and Terri Diane, 16 There was no hangar at Istanbul Airport that was big enough for a DC-10, so all maintenance work had to be done with the tail sticking out into the weather. Turkish Airlines Flight 981Infrastructural Failure of a DC-10. Passengers stuck at the airport as a result of the strike bought tickets to the first plane that could take them back to London, THY 981. As every policeman and firefighter in Senlis rushed into the Ermenonville Forest, Lannier didnt know what to expect. Mr, Yasuyuki Mohri, 23, city welfare employee wife Dorothy May, 51, company director Miss Erica Ann Sworder, 34, nurse The characteristics of the design of the mechanism made it possible for the vent door to be apparently closed and the cargo door apparently locked when in fact the latches were not fully closed and the lock pins were not in place. FAA Reauthorization Act; FAA Reauthorization Summary; #MH370 Definition of Underwater Search Areas Dec Speed! The sheer speed of the plane was causing lift to increase, thus raising the nose, but they werent pulling up fast enough. McDonnell Douglass response to this serious failure in testing was to make a few minor changes to the design of the door. This door was all but impossible to open in flight, but it necessitated a complex opening and closing mechanism which was difficult to design. 21 Turkish Airlines Flight 981 Photos and Premium High Res Pictures - Getty Images FILTERS CREATIVE EDITORIAL VIDEO 21 Turkish Airlines Flight 981 Premium High Res Photos Browse 21 turkish airlines flight 981 stock photos and images available or start a new search to explore more stock photos and images. Ten seats remained empty, but these too would have been filled if not for a bookkeeping error at the gate. What Is SID Standard Instrument Departure . When Mahmoudi learned that there was no more baggage to come, he closed the cargo door of the plane. and once more started to push the throttles forward, to level off. Among the passengers was Dr. Wayne Wilcox, a cultural attach of the Embassy of the United States in London, his wife, and two of his four children. Mr. William James Patrick Hayes, 50, married, six children, sals executive This caused damage to the fuselage, but not the explosive damage in the case of Turkish Flight 981. Mrs. Anna Philomena Middleton, 47, married, personnel director Shortly after this, legislation was thankfully passed to make the NTSB independent of the Department of Transportation.). Mr. Peter John Walsh, 23, lithographer Today, however, the engineer was away attending training, which meant that this duty fell to Engin Ucok, another ground engineer who was riding aboard the plane to service it during its stopovers. The result was that the DC-10 indeed flew before the L-1011 rolled, first taking to the skies on August 29th, 1970. The total failure of the floor severed all the control cables associated with the control surfaces in the tail. Mr. Mitsuo Yano, 23, bank management trainee Another plane, fuselage #47, was later found to have the exact same issues, indicating that it was not an isolated incident. [3][4] Among them were 17 English rugby players who had attended a FranceEngland match the previous day; the flight also carried six British fashion models, and 48 Japanese bank management trainees on their way to England, as well as passengers from a dozen other countries. In keeping with its overall design philosophy, Lockheed devised an ingenious system that turned the rear cargo door into a semi-plug door. The plane had landed at Orly Airport, Paris, where it was to drop off a group of passengers and continue on its way. After the disaster, the latches were redesigned and the locking system significantly upgraded. More ceiling panels came crashing down as they bounced over the grass, clattering into the aisles between rows of passengers hunched over in the brace position, expecting the worst. For at least six weeks the police were not even certain of how many people had died. And Turkish Airlines seemed like the easiest place to begin. Berkz tried increasing engine power, but he reversed his input as their speed increased toward 430 knots. In the case of Flight 96, the plane was able to make a safe emergency landing because not all of the underfloor cables were severed, thus allowing the pilots limited control. Five minutes after the crash, local police Captain Jacques Lannier was having lunch with his family at the Officers Club in the nearby village of Senlis when he received a phone call from his personal assistant: apparently a plane had gone down in the Ermenonville Forest. The plane crashed into the ground at a speed of about 800 km/h. _________________________________________________________________. At some point, one of the crew pressed his microphone button, broadcasting the pandemonium in the cockpit on the departure frequency. They had no rudder, barely any pitch control, one engine was dead, the master warning was blaring, and the cabin had depressurized. Mr. Robert G, Rcynaud, 43, married, tvro children, sales supervisor Mr. Tsukuru Yoshitake, 22, trading company management trainee, Mr. Penn Boyd Blair, 29, married, one child, machine company vice-president Mr. Gary Ray Chard, 36, married, four children, airline sales manager [2][8] Also on board was Georgina Forester, a model who had recently married and who was daughter of John Youens, the then-Chaplain-General of the British Army. Mr. Ian Roger Fuller, 24, fashion model Mr. Tctsuo Okura, 23, bank management trainee McGowen feared that an Airworthiness Directive, which is public and would be released to the media, might harm sales of the DC-10 relative to the L-1011. Indeed, the pilots immediately assumed that they had been involved in a mid-air collision; in their minds, it was the only possible explanation for so many simultaneous failures. The locking pins then ran into the sides of the flanges and stopped, the torque tube bent downward in the middle, the locking handle moved into the locked position, and the cockpit warning light went out. Mr. John Anthony Law-Wright, 33, married, two children, engineer and his wife Susan Vanessa, 28 Of course, he could not have known that the consequences would be fatal. An outward-opening cargo hatch is inherently less resistant to blowing open than an inward-opening one, also called a plug door. Mr. John North Lewis W1son, 25, married, research economist and his wife Joyce, 24, teacher Four of the five crew members and 62 of the 68 passengers were killed. Hurt to take his concerns about the DC-10s floor to McDonnell Douglas. (How baggage handlers were supposed to know whether they were applying more or less than 50 pounds of force was not explained.) He accelerated the engines back to full power, but the number two engine in the tail refused to respond. After Flight 96, McDonnell-Douglas added a small peephole that allowed the baggage handlers to visually inspect the pins, confirming they were in the correct position, and placards to show the correct and incorrect positions of the pins. Meanwhile, back in 1972, engineers at the Convair division of General Dynamics, which Douglas had contracted to manufacture the fuselage and doors according to its specifications, began to express concern about the design of the aircrafts floor. 177 passengers and four crew members came from the United Kingdom. The NTSB was also shocked by the FAAs refusal to implement its recommendations. While designing their respective airplanes, McDonnell Douglas and Lockheed took very different approaches to this problem. Crew of craft TC-JAV ( A detailed account here) Mr. Nejat Berkoz Mr. Mr. Julian Glynne Parish, 31, helicopter pilot Somewhere in this mad rush to get the planes ready, a critical step was missed: no one fitted fuselage #29 with the torque tube support plate or lengthened the maximum extension of its lock tube. In 1974, Bereaved families pray and look in utter horror at the devastation where the 300 ton DC-10 was reduced to small shards of twisted metal and personal effects scatted over a large area. Mr. Peter John Withers, 38, married, three children, company director Today, the story of the DC-10 cargo door and the suffering it caused is often oversimplified, reduced to the two accidents, the gentlemens agreement, and the Applegate memo. A blessing and a curse inward-opening one, also called a plug door from the United Kingdom the door any! Speed increased toward 430 knots by Turkish Airlines Flight 981 departure frequency error at the gate force was explained. 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turkish airlines flight 981 passenger list